Yes leakdown test was fine . We pulled heads and did a old fashion rod and piston check took a wooded hammer head put each pistion at tdc push down to see how much up and downplay we had . Set a dial indicator on zero at each pistion to see clearence found wound up being a bad bearing right before it would go where a rod bearing will only knock under a load if it fires car ran great but would not go over 6000 rpm st any shift