68 GT convertible project

Here is the last update. Now you'll be all caught up.

I'm still working on fitting the B&M shifter to the factory console. It looks like I'll be able to use the automatic console top plate after all. It will be a very tight fit but it should work. After taking the console in and out a bunch of times, I got tired of looking at the rusty mess inside the storage compartment. As you can see, the interior filled up with water on more than one occasion.
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I found a product called Iron Out under one of my sinks. It worked great for removing rust stains from a toilet so I thought I'd try it on the rust stained fiberglass of the console. It worked really well. Only a couple areas needed to be lightly sanded. Now all it needs is a couple light coats of SEM Landau Black.
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I'll need to have the driveshaft shortened for the 8 3/4 upgrade. The original shaft has two tapered ends on it. Since I don't know the exact driveshaft length I need, I didn't want to spend the time cleaning up the original shaft and then not be able to use it. I parted out a 76 Newport about 12 years ago and kept the driveshaft out of it. It's longer then the A-body shaft as well as a larger diameter.(3.5" instead of 3") It only has one tapered end so it should work fine for shortening. Here's what it looked like when I started.
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I put the shaft in a 5' piece of PVC pipe and filled it with vinegar. I checked the progress every 12 hours and gave it a light scrubbing with a scouring pad. It was in the bath for 36 hours. Here it is next to the Dart's original shaft.
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The metal will start to flash rust right away as you can see. I put the driveshaft back in the PVC but filled it with EvapoRust. The EvapoRust quickly removed the flash rust and does a great job and preventing it from returning immediately. The driveshaft soaked in the EvapoRust for under an hour. Then I rinsed it off, dried it and sprayed it down with WD-40. It should keep like this for quite awhile. Once I get the rear end mocked up, I can take my measurements and have it shortened.
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And finally, the other day I was looking for any other fasteners that needed to be cleaned up when I found this heater core tube plate that mounts in the engine compartment. It had seen better days so I made a new one out of some scrap.
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