tunnel ram update

Weather finally warmed up so I worked on the t-ram some more. Tried to adjust secondary door but had no real affect on the bog, just when it happened. So I changed jets. stock where 89 front and 98 rear. I went to 92 front and 107 rear. Man what a difference. Car runs even stronger and no more flat spot on the shift either. Still have a tiny bog if I stab it from an idle so I will adjust the air door again and see. Drives just as good as the rpm and preform 750 that was on it just way stronger from 4500 up. I am very pleased with the way it runs with as little tuning as ive done and it looks damn cool.


I'd bet you need bigger squirters. IIRC, Carter only had three sizes. Small, medium and large and I'd bet you have the small shooter. A medium squirter would clean all that stumble off idle right up.