Pro Flo 4 Timing

So I drove my car this weekend after installing the MSD adjustable rotor as others have talked about earlier in this thread. Night and day difference. Now I can get my cruising timing back to where it should be. It starts quicker, idles better, and my long and short fuel trims are lower than before. No more breakup above 3K rpm.

Also many have had an off idle stumble so I also replaced the TPS sensor and the off idle stumble is gone. Not sure if part is due to the rotor or not but most likely bad TPS.

This is how it should have run from the beginning.

That is good news. its strange the several pleaople also report this TPS sensor problem. what is the replacement part number just in case?

On the other hand, I oredered my adjustable rotor last week, will publish my experience as well, it should be similar to what other people has experienced here. In order to keep things okay I reduced my vacuum advance to 5 degrees only.