Thanks. I appreciate your thoughts. He explained it to me when I picked the the engine up. He said that when they were test running the engine, they monitor temperatures and noticed that it was running too hot. They then determined that it was a clogged j head, so they luckily had an exact date correct j head in inventory to swap it out with. He said that they still had no idea where or why mine was blocked, but that after swapping heads, the temps were good. He sent my old head home with me.