Kickdown issue

I'm not sure if it was rebuilt as a manual valve body. In any case, I have done my due diligence with the KD linkage adjustments so it's going to the shop to have them figure out why it isn't working. I was just curious if anyone has experienced this before.

The transmission was from a big block but was rebuilt into my small block casing. Unsure of the year of the 727.
We used to call the kick down, the passing gear. I never like to use it, but it did work. Reason was. there was a pause before the dropped gear change, so I would always manually, shift into 2nd or 1st as needed, for a more positive shift. I don't remember why, but I installed a nut and bolt on the slide on the other side of the slide stop, for a better down shift. If I remember correctly, about one inch ahead of the throttle linkage. It also sets the upshift. I could also be set to be in third gear around 20 up to 30-40.