Glad you got it! Compression Test would of told you this as well.I FOUND THE ISSUE!
so I was checking on a few things. Started with ignition advance. It's at 5* advance at 800rpm, and climbs almost to 20. so vacuum advance works.
I replaced my leaky bypass hose with 2 properly sized hoses and blocked them off with bolts.
Then as I was finishing up and filling it up with water, I decided to put some concentrate coolant in it, because sometimes it has additional cooling properties. With the engine running I noticed it puffing up out of the radiator... for some reason I NEVER saw this with just water.. sure enough, it's puffing A LOT and it was very hot air coming out of there.
So there we have it: a blown head gasket!
Picture 2 shows one of the puffs.
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Glad you got it! Compression Test would of told you this as well.
RadiatorOk.. headgasket done. Check out my "Disuster" thread for that..
... but.......
FAIL.... still getting hot!
What's your take on this: If I spray the radiator with water as it's running. the temp drops rapidly.
1. low water flow?
2. low air flow?
3. inefficient radiator?
Small update.. I PROMISE I will get to the rest of the stuff after this week.. but last night I drained what was in it.. the water came out medium brown in color - not as bad as I thought. So my heater core hose has a T-fitting with a cap half way to the firewall. I unscrewed that only to find it LOADED with gunk. I pulled off both hoses from the block and rinsed out some seriously nasty stuff. My guess is the Heater core was housing some of my problem. I ran a small bypass hose and am now running with no heater core.
So the test drive: It took a lot longer to warm up this time - I thought it was almost fixed til about 10 minutes in. then it got hot FAST. Like it hit a threshold. As I got home, the bypass hose that I made for the heater core was whistling, so I apparently did not get that tight enough.
more to come.
One more thing to think about. If it still has the original steel shim head gasket,. It's possible that the water jacket restrictions are rotted out which let's all the water come up from the block at the front of the head instead of the rear. Since it sounds like you have an infrared temp gun, just check the temp front to back. If it's way cooler at the front it may need a new head gasket. Also I've had blocks so plugged up with sediment that a garden hose wouldn't flush it out. I used a 1-1/2" gas powered water pump with no tstat in and just kept swapping top to bottom rad hoses until the water came out clean. Don't be surprised if you have a rusted out freeze plug after you're done.