NC Engine Builder
Grumpy Old Man
- Joined
- Oct 10, 2008
- Messages
- 6,447
- Reaction score
- 9,249
It went into valve float at just past 5800, the cam was a custom grind, and had extremely aggressive lobes. I went back into the heads and lightend up the retainers, and worked on the geometry a bit more, but the short installed height was extremely difficult to get a spring that worked. It added rpm to the powerband, but it didn't get put back on the dyno, as the customer was in need of getting it in the car